This month, we made the shell for the micro-mouse and modified some of the code so that the micro-mouse would follow the white line accurately. These were the last modifications before going to the scheduled date to test the micro-mouse that we had made. We faced some problems, such as the infra-red sensors, which were not working accurately. We found the problem to be that the sensors were very close to each other, so we had to move them farther apart. Finally, we prepared the presentation, put together the important points that we should talk about, and distributed parts of the presentation among the group members. On the day of the micromouse test, we did well and the results were as we expected.